Diesel World

P-PUMP CUMMINS TIMING

12 DEGREES OF TIMING TO 18 DEGREES--HOW MUCH WILL WE GAIN?

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We hear it all the time, timing makes power. But how much power? Well, there are a number of variables but it was a question we decided to try and answer with our pretty much stock 12v P-pump Cummins project Green Monster. In our last installmen­t we had put in a set of Scheid Diesel 5x0.018-inch injectors and gained a whopping 117 horsepower on the dyno. Since we were driving the turbo harder, boost also went from 19 pounds to 38 pounds which was part of our vast increase in power. To make the most of these new injectors though, we needed to add timing.

Injection timing in a diesel works very similar to the timing curve that you would find in a gasoline engine. One of the main difference­s however is that you can run a lot more tim

ing with boost in a diesel engine thanks to their direct injection and robust nature. The factory sets timing at 12 degrees, which is fine for cold startups noise concerns and overall power, but we wanted to tell the balance a bit towards the power part of the equation. This meant ramping up the timing well above our 12-degree starting point.

One of the main considerat­ions when it came to setting timing is that we were still on the stock 270,000-mile head gasket with factory re-tightened headbolts. We have run up to 30 degrees on trucks with ARP 625 head studs and fire ringed head gaskets but we would be limited (for now) by our factory parts. Many hot street trucks or folks that tow and want a little better mileage ought to go just a few degrees over stock which is what we did. We felt that a 5 to 7 degree bump would be adequate, and in the end we decided to go from 12 degrees up to 18 degrees of timing.

We had the folks at Brown’s Diesel help us in setting timing the “correct way” which is to use a dial gauge on the delivery valve holder. You’ll need the specificat­ions of your pump (160hp, 180hp, or 215hp) but as long as you have that you should be good to go. The actual process didn’t take that long, but it was good to have two people on the truck. We also marked one side of the crank position sensor to see how far it moved for those who may not have a dial indicator. The rumor was that moving the engine from one side of the crank sensor

pickup to the other with the pump gear off was worth about 10 degrees, as it turned out, the Internet was close, and it actually turned out to be closer to 12 degrees.

Once on the dyno the truck was a little louder, but nothing that bad, and cold start and other driving aspects of the truck remained unchanged. It should be noted that we did have to adjust the idle up which was performed at the back of the pump with a 19 mm wrench. On the dyno, we were quite pleased with the power game, as we picked up an additional 30 horsepower over what we had made with just the injectors alone. The additional timing also actually made the boost drop from 38psi to 35psi so in an apples to apples comparison the extra six degrees of timing may have been worth even more than 30 horsepower. With 400 in sight, our next move will to be to install a lift pump from Power Driven Diesel to see if we can break the 400rwhp mark. As for now, we learned that even six degrees will make quite a difference in power, and in our case was worth almost 10 percent!

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 ??  ?? The timing pin is removed, and will be reinstalle­d backwards later in order to hold the pump at a set timing. But for now we just needed to remove it. If you’re worried about breaking the small plastic pin (which can happen if you’re not careful) metal ones are available from various vendors.
The timing pin is removed, and will be reinstalle­d backwards later in order to hold the pump at a set timing. But for now we just needed to remove it. If you’re worried about breaking the small plastic pin (which can happen if you’re not careful) metal ones are available from various vendors.
 ??  ?? Our first step of our timing change involved removing a 24mm cap and removing a small plastic “bullet” that is used to pin the pump so it won’t move. A small amount of oil will come out which is ok, since it will be replenishe­d as soon as the truck is restarted.
Our first step of our timing change involved removing a 24mm cap and removing a small plastic “bullet” that is used to pin the pump so it won’t move. A small amount of oil will come out which is ok, since it will be replenishe­d as soon as the truck is restarted.
 ??  ?? Moving up to the top of the engine, we loosened the #1 injection line from the clamps and bent it slightly in order to clear the pump’s delivery valve. If you don’t feel like bending the line you can always just remove it.
Moving up to the top of the engine, we loosened the #1 injection line from the clamps and bent it slightly in order to clear the pump’s delivery valve. If you don’t feel like bending the line you can always just remove it.
 ??  ?? Next we removed the back #6 valve cover so we could see the rocker arms and then turned the engine backwards by the alternator to get close to TDC. With the valves on #6 on overlap (the rockers are crossing each other rising and falling) #1 should be close to Top Dead Center (TDC) on the compressio­n stroke, which is where we’ll need it to check timing.
Next we removed the back #6 valve cover so we could see the rocker arms and then turned the engine backwards by the alternator to get close to TDC. With the valves on #6 on overlap (the rockers are crossing each other rising and falling) #1 should be close to Top Dead Center (TDC) on the compressio­n stroke, which is where we’ll need it to check timing.
 ??  ?? Next we used a specialty delivery valve tool to remove the delivery valve from the pump, which will come out in a number of pieces. Don’t lose any of these! Or get them dirty.
Next we used a specialty delivery valve tool to remove the delivery valve from the pump, which will come out in a number of pieces. Don’t lose any of these! Or get them dirty.
 ??  ?? Back up on the top of the pump, we put the dial indicator at a high number and rotated the engine backwards until the pointer stopped dropping. This meant the dial indicator is at the back of the pump cam lobe. From there, we zeroed out the dial indicator at 0.0 to find timing via plunger lift.
Back up on the top of the pump, we put the dial indicator at a high number and rotated the engine backwards until the pointer stopped dropping. This meant the dial indicator is at the back of the pump cam lobe. From there, we zeroed out the dial indicator at 0.0 to find timing via plunger lift.
 ??  ?? From 0.0 lift, we rotated the engine forward until it reached TDC, which was measured at 5.6mm of lift, or about 12 degrees. Since factory timing was listed at 12.5 deg on our truck, we knew we were very close to TDC.
From 0.0 lift, we rotated the engine forward until it reached TDC, which was measured at 5.6mm of lift, or about 12 degrees. Since factory timing was listed at 12.5 deg on our truck, we knew we were very close to TDC.
 ??  ?? We marked TDC on the balancer on either side of the crank sensor with a screwdrive­r for future reference, and to see how much the damper would turn when our pump was re-timed.
We marked TDC on the balancer on either side of the crank sensor with a screwdrive­r for future reference, and to see how much the damper would turn when our pump was re-timed.
 ??  ?? After we found TDC, the oil filler was taken off, which gave us access to the large timing pump gear nut.
After we found TDC, the oil filler was taken off, which gave us access to the large timing pump gear nut.
 ??  ?? Technician Erick Brown mounted a dial indicator on the pump that extended down into the pump and measures pump camshaft lift. This will be used to determine timing.
Technician Erick Brown mounted a dial indicator on the pump that extended down into the pump and measures pump camshaft lift. This will be used to determine timing.
 ??  ?? When we got close to TDC, we took the valve cover off the number 6 cylinder and had one mechanic go under the truck and turn the engine slowly by the flywheel teeth until the rockers crossed over. This meant cylinder number one would be on the top of the compressio­n stroke. Other popular methods of finding tdc are pushing on the timing pin right below the injection pump, or using a dial indicator set to the piston on the number 1 injector hole.
When we got close to TDC, we took the valve cover off the number 6 cylinder and had one mechanic go under the truck and turn the engine slowly by the flywheel teeth until the rockers crossed over. This meant cylinder number one would be on the top of the compressio­n stroke. Other popular methods of finding tdc are pushing on the timing pin right below the injection pump, or using a dial indicator set to the piston on the number 1 injector hole.
 ??  ?? With the pump now advanced six degrees, we tightened the gear back down to 20 lb-ft to seat the gear, then pulled the timing pin, held the engine with the barring tool, and tightened it to a final torque of 144 lb-ft.
With the pump now advanced six degrees, we tightened the gear back down to 20 lb-ft to seat the gear, then pulled the timing pin, held the engine with the barring tool, and tightened it to a final torque of 144 lb-ft.
 ??  ?? After the pump gear was installed, we removed the dial indicator, and reattached the injection pump line and engine intake.
After the pump gear was installed, we removed the dial indicator, and reattached the injection pump line and engine intake.
 ??  ?? Since we hadn’t installed gauges yet, we installed a couple makeshift ones for fuel pressure and boost so we could gather some accurate data.
Since we hadn’t installed gauges yet, we installed a couple makeshift ones for fuel pressure and boost so we could gather some accurate data.
 ??  ?? After pinning the pump, we turned the engine back to our TDC marks, so that the pump would now be timed at 18 degrees of timing.
After pinning the pump, we turned the engine back to our TDC marks, so that the pump would now be timed at 18 degrees of timing.
 ??  ?? We continued moving the pump to 6.8mm of lift, or approximat­ely 18 degrees before pinning the pump (with the plastic pin shown in the third photo) and then pulling the injection pump gear with a gear puller. A barring tool was used to secure the engine in place so the timing pin wouldn’t break when the gear was broken loose.
We continued moving the pump to 6.8mm of lift, or approximat­ely 18 degrees before pinning the pump (with the plastic pin shown in the third photo) and then pulling the injection pump gear with a gear puller. A barring tool was used to secure the engine in place so the timing pin wouldn’t break when the gear was broken loose.

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