Motor Equipment News

Diagnostic­s

- By Peter Leijen, BE(Hons), Applicatio­n Engineer, for AECS Ltd.

The problem presented to the help desk: a 2008 Nissan Vanette CR diesel with a misfire at about 1,300–1,500rpm. This article is complex and needs detailed reading for full understand­ing – enjoy! I will run through all the data that was presented, explaining the diagnostic steps that we take when running through a complicate­d problem like this seemingly simple issue.

Where to start?

When presented with a misfiring engine we want to distinguis­h between two different scenarios. 1. Fixed misfire on one (or more) cylinders. 2. Random misfire. First, we want to see an ATS scope recording of the crankshaft sensor signal and an injection signal.

The injection signal gives us a reference as to which cylinder is having an issue, or if the issue is across multiple cylinders. Recording the crankshaft sensor signal also shows the quality of the signal i.e. is it corrupted with noise, etc.

Zooming in on the crankshaft pattern showed that there is no noise on the pattern so this will not be the cause of the misfire. The recording of crank vs injection with the calculated rpm line shows that there are multiple misfires occurring which seem to be linked to two cylinders. Based on the firing order we can see that cylinders 1 and 2 are misfiring.

EGR?

Random misfires are usually caused by air flow issues i.e. an EGR valve that is not functionin­g properly. We blocked off the EGR valve, but this made no difference to the misfiring of the engine. It must be noted that blocking the EGR valve also disrupts swirl in the engine. The ignition dampening effect of the CO2 in the exhaust gasses has been removed, so as a result the engine sounded more rattily.

We can now safely say that the EGR is not the cause for the misfiring engine, and that we are happy with the gas flow through the engine. Just to be doubly sure a relative compressio­n test was also performed which showed that all four cylinders were within two percent of each other, a perfect result.

Compensati­on values.

Having eliminated the crankshaft sensor, EGR valve and compressio­ns, it is time to look at the injectors. This Nissan Vannette (RF-T engine) is the result of a joint operation between Mazda and Nissan. As a result, we had with the scan tool access to the injector compensati­on valves, which is something the designers at Nissan do not give you access to on, for example, their Navara.

The injectors are compensate­d at four different pressure set points to ensure that the engine is running smoothly under different conditions. The graph in figure 3 shows these set-points and the compensati­on values of each cylinder.

These adaption values were recorded with a Launch Scantool and sent to AECS for analysis with our own software.

Please note: this level of support, and being able to share data is something that is unique to the AECS help desk.

Figure 3 shows the four set-points at 35, 65, 100 and 140 MPa rail pressure. This graph instantly shows that there is an issue with injector number four because its adaption values lie so much higher than the other three injectors. However, our crankshaft speed measuremen­t did not identify no.4 as a misfiring cylinder.

Closing the loop

I regard the automotive sector in New Zealand as being highly skilled, and not simply parts Swappers, so let us look further. Please put your thinking cap on, brew another coffee, and step into our world!

All four injectors were removed and tested by a local diesel specialist, who shared thedata with us, thank you.

A scanned copy of the results was sent to us and the data was a real eye-opener! The table presents the results.

The tables need some explaining. The actuation time, pressure, measuremen­t time, set injected quantity and set return quantity are all specified by the manufactur­er.

For example if these injectors are tested for a full load test they need to be activated for 860us at a pressure of 160 MPa for 120 seconds, and the actual injected quantity should be between 51.8 and 58.8 mm3/H (ccs per stroke), with a fuel return quantity between 0 and 86 mm3/H.

These tests have confirmed what the adaption values have already told us. Injector number four is faulty. As a result, the diagnostic­ian replaced just injector number four.

Based on the scope patterns it is needless to say that replacing just injector no.4 did NOT improve the running of the vehicle.

What is injector compensati­on?

To answer this question we need some more data from the vehicle. The recording shows rpm, Inj4 and suction control valve duty-cycle.

When the suction control valve duty-cycle increases, more fuel enters the rail, when the control valve duty-cycle decreases less fuel enters the rail. Figure 4 highlights three important areas.

#1. The duty-cycle increases after a misfire has occurred. The ECU sees that the crankshaft has slowed down and now wants to speed up the crankshaft again. This is done by injecting more fuel in the following cylinder.

#2. The duty-cycle decreases after injector four injects. This is because injector four has higher than normal leakage rate (see test sheet table). #3. This is the same cylinder as in #1, but now we don’t see the increase in duty-cycle. This is because the cylinder beforehand fired properly so there is no need to speed up the crankshaft with

additional fuel. In this duty-cycle pattern, we can see two mechanisms at work. We can see the ECU compensati­ng for a sudden decrease in crankshaft speed and we can see the ECU compensati­ng for an injector with high return flow (rail pressure decrease).

Conclusion

Looking back at the injector tables we can see that the return flow of injector #2 under the leak test is more than twice that of injector #1, but further from the set-point. Similar conclusion­s can also be drawn with the other injectors.

As a result, we replaced all four injectors. The car was returned to the customer who took it for a 1,000km drive, and then bought it back into the workshop to have the injector compensati­on values re-checked. Figure 5 shows the before and after results. We can see that Injector one did not need replacing, because the compensati­on values did

not move as far as the other three injectors.

It also needs stating that we get more and more customers who purchased other brands of scopes, asking for our technical support. We try to help as much as we possibly can, but this usually ends up in a DNF (racing terms for “did not finish”) job. This is most frustratin­g for us and our customers.

Please make sure you choose your knowledge and equipment partner wisely.

Both you and AECS are dealing with more complex problems daily. AECS has the ability and resources to simplify these complex problems in an easy to understand manner for your benefit.

 ??  ?? Figure 1: ATS scope recording of crank vs injection showing misfires.
Figure 1: ATS scope recording of crank vs injection showing misfires.
 ??  ?? Figure 3: injector set-points and adaption values.
Figure 3: injector set-points and adaption values.
 ?? READER REPLY 0140841 ?? Figure5: before and after replacemen­t injector compensati­on results.
READER REPLY 0140841 Figure5: before and after replacemen­t injector compensati­on results.
 ??  ?? Figure 4: ATS 5004d scope recording of inj, SCV duty cycle, and RPM.
Figure 4: ATS 5004d scope recording of inj, SCV duty cycle, and RPM.
 ??  ?? Figure5: before and after replacemen­t injector compensati­on results.
Figure5: before and after replacemen­t injector compensati­on results.
 ??  ?? Figure2: relative compressio­n test.
Figure2: relative compressio­n test.

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