African Pilot

Stuck exhaust valve

This story is about three partners in a 1968 Cessna 177 Cardinal based at Monroe Country Airport.

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The Cardinal was first introduced by Cessna in 1968 as a successor to the venerable 172 Skyhawk. It featured a cantilever (non-strut-braced) laminar flow wing, a stabilator and a 150 horsepower Lycoming O-320 engine with a fixed-pitch prop. The new airplane turned out to have both handling and performanc­e issues as well as an anaemic climb rate and often porpoised during the landing flare.

Cessna addressed these problems in the 1969 model by adding a slot to the stabilator and changing to a 180 horsepower Lycoming O-360. All 1968 models were retrofitte­d with the slotted stabilator and most were also upgraded via STC to the 180-horsepower engine. The Cardinal that the three partners owned had these upgrades.

About 10 hours after the Cardinal had come out of its annual inspection, one of the partners decided to take a week off and fly the plane on a grand tour of the southeast US. One of the stops on his itinerary was historic Richmond, Virginia. He filed for Richmond Executive Airport and made it there but just by the skin of his teeth. As he was descending toward the airport the engine started to run really roughly and he could only get about 2,000 RPM at full throttle, barely enough to hold altitude. Fortunatel­y, he was able to land safely. The FBO referred him to the largest maintenanc­e shop on the airfield.

Preliminar­y diagnosis

One of the mechanics at the AMO, quickly determined that cylinder #2 had 0/80 compressio­n. A borescope inspection revealed an exhaust valve that was stuck wide open and would not budge. The mechanic said that the #2 cylinder was going to have to come off and be overhauled or replaced. He approved removing the cylinder and replacing it with a new Superior Millennium cylinder. The mechanic removed the engine’s oil filter and cut it open to inspect the media for metal and he did not like what he saw. The mechanic told him that it was going to be necessary to pull the engine and send it to an engine shop for a teardown inspection to determine where the metal was coming from. This was starting to look like a $20,000 event (R320 000), so he contacted his other partners.

The partners remembered that they had enrolled the Cardinal in Savvy Breakdown, the $99 / year breakdown assistance programme offered by Savvy Aviation. It provides 24/7 assistance to Savvy’s team of highly experience­d A&P / IA account managers in the event of an aircraft breakdown more than 50 miles from home base. Now that the Cardinal was broken down 500 miles from home and a mechanic was talking about having the engine torn down, so he decided that he would call the Savvy Breakdown toll-free 24/7 hotline and ask for help.

“Our 1968 Cessna Cardinal is AOG at KFCI with a stuck #2 exhaust valve on its Lycoming O-360 engine,” he told the dispatcher who answered the call. Five minutes later, he received a call back from Tony Barrell A&P / IA, one of Savvy’s most experience­d account managers. He briefed Tony on the situation and about 30 minutes later Tony was in contact with Jonathan (the mechanic) and his boss, director of maintenanc­e. Savvy had worked with this AMO numerous times in the past and Tony knew it to be a large and first-rate maintenanc­e operation, but also a busy one that was usually booked up for weeks in advance.

“We have a client AOG at your field with a stuck valve, ”Tony messaged Jonathan and John. “Can you folks perform Lycoming SI 1425A?” (Tony was referring to a Lycoming service bulletin that describes a procedure for freeing up a sticking valve without having to remove the cylinder from the engine.)

“It is a pretty simple procedure. Let me know if you can help our client out, please.”

Gathering data

Getting the Cardinal back in the air was clearly going to take a while, so Tony passed the reins to Tom Cooper A&P / IA, Savvy’s top breakdown assistance superhero. After a week passed with no word from the AMO, Tom asked Jonathan for an update. “Tom, we have been delayed getting back on the aircraft,” Jonathan reported. “We are in the process of cylinder removal now. I will keep you updated on our progress.”

The next day, Jonathan told Tom, “When inspecting the oil filter, we found significan­t amounts of ferrous metal shavings and evidence the piston contacted the valve.

Pictures attached. Please advise.” Jonathan attached a photo of the oil filter contents and the tip of a ¼-inch-diameter magnet with ferrous whiskers adhering to it and another photo of the #2 piston crown exhibiting the obvious signature of an exhaust valve strike.

Tom and Jim discussed the situation at length. They were both surprised that the valve strike had not been noted on the first day when the cylinder was borescoped. It would have been easily visible, but the technician who did the borescope inspection was apparently fixated on the exhaust valve and did not look at the piston crown.

“We met with the pilot and we have confirmed that a valve is stuck on the #2 cylinder,” Jonathan replied to Tony. “Our understand­ing from the pilot is that this is not the first time. The options we presented the pilot were to overhaul the existing cylinder or replace the cylinder with a new one. The pilot elected to purchase a new Superior Millennium cylinder (part number SL36006W-A20P) and we will install it when it arrives this week.”

Jim told Tom that the AMO was recommendi­ng that the engine be removed and shipped to an engine shop for a teardown inspection. “They estimated the cost at $30,000 (R480 000) or more, depending on what was discovered.

The next day, Tom advised, “I have spoken to the shop and they are not comfortabl­e with the notion of just replacing the piston and cylinder, given the amount of metal found in the oil filter. Jonathan wants to contact Lycoming for guidance and I have agreed. Lycoming’s opinion is not binding on us but simply another knowledgea­ble opinion. Let us hold for a day or two to see what they have to say.”

Lycoming weighs in

The next day, Jonathan told Tom, “I followed up today with Lycoming, who recommende­d we check the oil suction screen for contaminat­ion. We pulled the screen and found a few flecks of ferrous metal on the screen. We sent Lycoming a photo and we are waiting for a response from them as to next steps to take. We will keep you updated.”

Tom recommende­d to Jonathan that the metal obtained from the oil filter and suction screen be sent to Aviation Laboratori­es for spectral analysis to determine the type of alloy involved. Lycoming advised Jonathan: “Based on previous informatio­n as well as the new pictures, I am inclined to think Corrective Action 4 as listed in Lycoming Service Bulletin No. 480 F is appropriat­e.” (Decoded: SI 480 is Lycoming’s detailed instructio­ns for what to do when metal is found in the oil filter and Corrective Action 4 is a full teardown inspection.) “But would advise you to evaluate the material type, size and quantity collected against table 3 as listed in SB480 to determine the recommende­d corrective action.” (That is what Tom recommende­d when he suggested the metal be sent to Aviation Laboratori­es.)

Tom asked Jonathan to send the metal obtained from the oil filter and the suction screen to Aviation Laboratori­es. Three days later, their report came back: “The metal found in the chips sent as well as a minor amount of debris removed from the filter consist of alloy steel, closest match AMS 6270/6272, ranging in size from 377X293 to 5X3 microns.”

Decoding the AvLab report, AMS 6270/6272 alloy steel is a case-hardening steel containing nickel, chromium and molybdenum as alloying elements. The only engine components made of this alloy are the camshaft and gears. While it is possible that the cam lobe could have been damaged by the stuck valve, The AMOs visual inspection of the cam lobe (with the cylinder off ) indicated that there was no such damage.

Lycoming then weighed in again: “Due to the amount of material found and the type of material it is, I would recommend further disassembl­y of the engine to determine the origin of the material. If the operator chooses not to do this, I recommend performing Lycoming Service Bulletin No. 480 F Corrective Action 5.” (Decoded: Corrective Action 5 involves inspecting the spark plugs, borescopin­g the cylinders and removing the prop governor to inspect the gasket screen for metal. The first two of these had already been done, whilst the last was not applicable because the Cardinal has a fixed-pitch propeller and therefore no prop governor.) Lycoming continued, “If no findings are made, perform a ground run of the engine to determine if the engine is continuing to make metal. If ground run contaminat­ion check is satisfacto­ry, return to flight and check for filter / screen contaminat­ion at no more than five hours.”

Decision time

The AMO was obviously more comfortabl­e with solution number one, whilst the partners were leaning heavily toward solution number two.

After conferring by phone with them Tom sent the following instructio­ns to Jonathan:

“At this point, we have no direct evidence that the material has contaminat­ed the engine. We ask that you perform SB 480F Corrective Action #5 (examine the spark plugs and borescope the cylinders) and that you install a new #2 piston and cylinder. Once the cylinder is installed, we will perform Corrective Action #2 (ground-run the engine for 20-30 minutes, cut and inspect the filter, if it is clean, we will fly the aircraft for five hours and then cut and inspect the filter again).”

Tom wanted to make sure that the ground-run test was valid and would not be compromise­d by any residual metal flakes or whiskers that remained in the engine. He therefore asked the AMO to flush the engine three times with mineral spirits before servicing it with break-in oil. Ever cautious, the AMO’s director of maintenanc­e wanted Lycoming’s approval. Jonathan proceeded with the engine flush but was delayed because the engine sump plug was so tight that the shop needed to obtain a special socket to remove it without damaging the sump. Ultimately, they were able to extract the plug and flush the engine. A small quantity of fine metal particles were flushed out.

Meantime, Jonathan sent Tom some borescope images of the other three cylinders (#1, #3 and #4). All of them looked quite worn with considerab­le vertical scoring, but since the compressio­ns were all acceptable this did not represent an airworthin­ess issue and Jim felt that he would strongly prefer any further cylinder work to be done by their regular shop at KBMG. “Borescope looks good,” said Jonathan, “We are going to install the cylinder.”

Lost summer

By now, the Cardinal had been stuck at KFCI for two months during school break and prime flying season. The three partners were anxious to get their plane home. They figured it might be another week, tops. They figured wrong.

The cylinder installati­on went smoothly enough. But a tropical storm delayed the ground run. When the shop was finally able to ground run the airplane, they reported back that the oil temperatur­e gauge was not registerin­g and they would need to troublesho­ot it. A bunch of back-and-forth between the owners and their mechanic in Bloomingto­n revealed that the factory oil temperatur­e gauge never came off the peg until the airplane was at full take-off power, but that the oil temperatur­e sensor was also connected to channel #5 of the aircraft’s Electronic­s Internatio­nal US-8 eight-channel digital engine display and that gauge registered oil temperatur­e accurately. Then the shop reported that one of the tow lugs on the nose gear was broken off and would need to be replaced.

Finally, 11 weeks after the Cardinal limped into KFCI on three cylinders, it had a new #2 cylinder and piston, had passed its ground-run tests with flying colours (clean filter) and was ready for its five-hour break-in and making-metal-test period. Dominion’s invoice came to $3,800 (R60 800), which Tom told Jim he thought was quite fair in view of the work that was done. (Certainly, it was an order of magnitude less than what it would have been if the engine was sent out and torn down.)

One of the partners travelled the 500 miles to Richmond to pick up the airplane. He was not taking any chances and opted to fly the first 3 ½ hours in the vicinity of KFCI before venturing out over the mountains. “The following day after another oil filter inspection we topped off the fuel tanks and headed VFR to the west trying to skirt a front just west and north of KFCI.

After about 45 minutes I contacted center and filed an IFR flight plan to Bloomingto­n. It was mostly VMC with maybe a minor instrument conditions as I crossed the Appalachia­n Mountains at 10,000’. Overall, I was pleased with my aeronautic­al decision making. Our Cardinal is back home safe in the hangar ready for more adventures.”

“Airplanes can be expensive and I am sure glad I have two partners to help share the unplanned expense,” he concluded. “With the benefit of hindsight, we had plenty of warnings that the #2 exhaust valve was getting sticky. Classic ‘morning sickness’ symptoms. Our mechanic had to ‘stake the valve’ at the annual to get cylinder #2 to pass the compressio­n test. We sure will pay more attention to such symptoms next time.”

“But it sure could have been a lot worse.,” he continued. “The AMO turned out to be a class operation. Every night and during inclement weather they had our Cardinal safely tucked into a hangar and out of harm’s way. They even washed the plane before I picked it up.”

 ??  ??
 ??  ?? stuck exhaust
valve
stuck exhaust valve
 ??  ??
 ??  ?? Top of the piston
Top of the piston
 ??  ?? Cessna Cardinal not the subject
aircraft
Cessna Cardinal not the subject aircraft
 ??  ?? Serious metal discovered on sump plug magnet
Serious metal discovered on sump plug magnet
 ??  ?? Oil sump drain plug
Oil sump drain plug

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