Engineering in Miniature

HARRY’S GAME – 6-INCH REGULATOR REFURB

Maintenanc­e of a 6-inch scale go-valve occupies our resident engineer in this month’s look behind the shed door at the Fairbourne Railway.

- By Harry Billmore

The last few weeks in the lockdown-induced quiet surroundin­gs of the Fairbourne Railway workshop have seen me mainly focusing on the continuing 10-year overhaul of our Darjeeling style 0-4-0ST ‘Sherpa’, and after disassembl­ing the boiler and its internals, it was time to take a good look at the regulator.

Checking the maintenanc­e records there had been no reports of a leaky regulator from the drivers over the past season so I wasn’t expecting anything too bad, and this was confirmed after I stripped the regulator down fully – neither of the mating faces were particular­ly scored or pitted which was a good sign. There were just the usual wear marks from use, however with the regulator out of the boiler I took the opportunit­y to reface it and lap it in to hopefully give another 10 years of trouble-free use.

The design is a nice simple rotating disc regulator, with three teardrop ports spaced equally around the mating face, giving nice proportion­al control. There is a replaceabl­e bronze insert in the moving half and the stationary section is a piece of cast iron, with a replaceabl­e mating face too.

I started the job by setting up the stationary section in the four-jaw chuck of the lathe and faced across the sealing face of the regulator – this removed the little bit of pitting and grooving that had occurred.

Figure of eight

I then went over to the surface plate and with the usual figure-of-eight motion on some Wet and Dry paper, polished the machining marks out of the cast iron. Using a figure-eight motion prevents any bias occurring in the polishing, wearing down one side faster than another.

Unfortunat­ely the countersun­k screws that are used to hold the replaceabl­e face on the valve are at the surface of the cast iron. Since these are harder than the iron they will wear the bronze more, but this shouldn’t be an issue as it should simply wear a circular section of the bronze and not between any of the port faces.

To get an idea of how much material I would need to take off the bronze face, I quickly rubbed this over on the surface table as well and you

can see the results in the pictures.

This necessitat­ed making a couple of passes on the lathe before it was back to the surface table for final finishing.

The regulator was then reassemble­d, rememberin­g to put PTFE tape on the central pivot to prevent leaks as it goes between the steam space of the boiler and the regulator J-pipe. I tensioned the spring to ensure it held the faces together but still allowed for nice easy operation.

I then re-assembled this onto the components of the J-pipe that sits in the dome and set it aside until the boiler has been re-tubed.

Regulator gland

When I took the regulator gland off Sherpa, I discovered that it was past its best, with a corroded bore that had started to mark the stainless regulator rod, and a corroded end which squeezed the regulator gland packing out around the gland rather then compacting it to seal on the regulator rod.

All of this encouraged me to replace the gland, and to replace it with an SAE660 bronze one at that. Unfortunat­ely we did not have any castings lying around for this gland so it would have to be machined from solid and again I ran into a problem – the only stock material we had that was big enough to machine the bolting flange from was not thick enough to machine the full length of the gland. As a result I was forced to fabricate the gland from two pieces.

The first task was to machine the centre section that the regulator rod runs through. I turned the outer diameter to fit into the gland housing before boring out the bore to be a good sliding fit on the regulator rod.

I machined the face that compresses the gland with a taper on, to help compress the packing material onto the regulator rod. Once this was complete, I turned it around and machined the main diameter down to 10mm bigger than the cored section of the large diameter bronze stock.

Safety step

I then machined a step into the front face of this so that if the braze ever did fail, the centre section that has the pressure acting on it would be held in place by the matching step on the outer bolt flange.

After the inner section was machined to size, including putting weld preps on the outer facing surfaces, I put the larger piece of bronze into the chuck, faced it off and then bored the middle to fit around the centre section, including the emergency step.

I couldn’t do any more machining to this piece as it was too thin to turn

the outer diameter so I took the piece out of the lathe and then Tig-welded the back side of the gland up. This is a very similar technique to Tig-welding steel, it just happens to be in bronze in this case – you can use a variety of filler rod, but I used some SAE660 to be a perfect match with the base metal.

After completing the welding I put the gland back into the lathe, holding it on the outer bore of the smaller diameter, allowing me to machine the front face and outer diameter of the bolting flange.

I machined it down until the thickness of the flange matched the end of the centre section, with the small weld prep visible. I then Tig-welded the front face before cleaning this up on the lather again.

If it looks right...

Next job was to mount the flange in the rotary table on the mill and drill the two bolt holes into it, before milling it to the final shape that I liked onto the outside. I did this by drawing the shape I wanted with a Sharpie pen onto the bronze, then rotating the table until the drawing was perpendicu­lar to the table.

Having machined this edge, I rotated the table by 180 degrees to get the parallel edge. I then added the angle the table was sat at to the original angle the table had been at to then produce the lozenge shape.

This was then further finished by roughing the radius at the top and bottom by determinin­g by eye where the cutter touched the gland and using the table to machine the radius, then lowering the table, turning the table through 180 degrees and taking the same cut. Once this was done, I finished the radii off with a file, completing the new gland.

To go alongside the gland, I mounted the regulator rod in the lathe and skimmed the length that sits in the gland to remove the pitting and roughness left by the previous gland, finishing this off with a piece of emery cloth to leave a good polished surface for the new gland material to run on. Another job of the many in a 10-year overhaul done!

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PHOTO 1: Start – bronze moving section of regulator as taken off boiler.
1 PHOTO 1: Start – bronze moving section of regulator as taken off boiler.
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PHOTO 3: Polishing casting face using coarse Wet and Dry on surface plate.
3 PHOTO 3: Polishing casting face using coarse Wet and Dry on surface plate.
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PHOTO 2: Turning casting face, only skim needed as shown by original face in centre.
2 PHOTO 2: Turning casting face, only skim needed as shown by original face in centre.
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PHOTO 5: More time on coarse Wet and Dry improves surface.
5 PHOTO 5: More time on coarse Wet and Dry improves surface.
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PHOTO 4: Results of coarse paper, note slight chatter where tool tip caught steel fasteners.
4 PHOTO 4: Results of coarse paper, note slight chatter where tool tip caught steel fasteners.
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PHOTO 7: Fine Wet and Dry used to polish to even finer finish.
7 PHOTO 7: Fine Wet and Dry used to polish to even finer finish.
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PHOTO 6:
Finish with coarse Wet and Dry.
6 PHOTO 6: Finish with coarse Wet and Dry.
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PHOTO 8: Skim across bronze section turning face to speed up finishing.
8 PHOTO 8: Skim across bronze section turning face to speed up finishing.
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The regulator reassemble­d and mounted back on upright section of J pipe.
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PHOTO 13: The regulator reassemble­d and mounted back on upright section of J pipe. 13
 ??  ?? PHOTO 9: First quick rub on coarse Wet and Dry reveals high spots.
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PHOTO 9: First quick rub on coarse Wet and Dry reveals high spots. 9
 ??  ?? PHOTO 11: Back to surface plate to finish face – tool tip has polished a little, not a worry when hand finishing to be done after.
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PHOTO 11: Back to surface plate to finish face – tool tip has polished a little, not a worry when hand finishing to be done after. 11
 ??  ?? PHOTO 17: Checking fit of centre piece, note weld prep.
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PHOTO 17: Checking fit of centre piece, note weld prep. 17
 ??  ?? PHOTO 15: After parting off bulk of waste material from centre section.
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PHOTO 15: After parting off bulk of waste material from centre section. 15
 ??  ?? PHOTO 14: Comparing the diameters of two pieces of bronze available to make new regulator gland. The upper one will form the bolting flange.
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PHOTO 14: Comparing the diameters of two pieces of bronze available to make new regulator gland. The upper one will form the bolting flange. 14
 ??  ?? PHOTO 10: More work on surface table shows deeper scores accross sealing face.
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PHOTO 10: More work on surface table shows deeper scores accross sealing face. 10
 ??  ?? PHOTO 12: Final finish achieved.
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PHOTO 12: Final finish achieved. 12
 ??  ?? PHOTO 18: The two parts ready to be welded together.
All photos in this feature by the author
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PHOTO 18: The two parts ready to be welded together. All photos in this feature by the author 18
 ??  ?? PHOTO 16: Machining a step in to take pressure in case weld ever fails.
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PHOTO 16: Machining a step in to take pressure in case weld ever fails. 16
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PHOTO 26: Comparison between front of old and new gland, note oil hole in new one, this will extend life of packing material and make moving regulator easier.
26 PHOTO 26: Comparison between front of old and new gland, note oil hole in new one, this will extend life of packing material and make moving regulator easier.
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PHOTO 24:
Bolt holes drilled on rotary table, original gland for comparison.
24 PHOTO 24: Bolt holes drilled on rotary table, original gland for comparison.
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PHOTO 28: Turning regulator rod to clean it up, note corrosion caused by the old gland.
28 PHOTO 28: Turning regulator rod to clean it up, note corrosion caused by the old gland.
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PHOTO 21: The front weld completed.
PHOTO 22: Machining back the front weld.
22 PHOTO 21: The front weld completed. PHOTO 22: Machining back the front weld.
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PHOTO 19: First weld made on back of gland, note chamfer on centre piece to help seal gland packing.
19 PHOTO 19: First weld made on back of gland, note chamfer on centre piece to help seal gland packing.
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PHOTO 20: Bolting flange machined to final thickness, note weld prep.
20 PHOTO 20: Bolting flange machined to final thickness, note weld prep.
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PHOTO 27: Looking at rear, note shape of inner edge of original and the corrosion.
27 PHOTO 27: Looking at rear, note shape of inner edge of original and the corrosion.
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PHOTO 25: Lozenge shape machined mostly by eye, aiming for something that looks right.
25 PHOTO 25: Lozenge shape machined mostly by eye, aiming for something that looks right.
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PHOTO 23: Front weld after machining back.
23 PHOTO 23: Front weld after machining back.
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PHOTO 29: The final touch – regulator rod polished with emery cloth.
29 PHOTO 29: The final touch – regulator rod polished with emery cloth.
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