Daily Press

Mechanical failure caused Navy copter’s fatal crash

Investigat­ors: Pilots were not at fault for San Diego accident

- By Erika I. Ritchie

A Navy investigat­ion says an August helicopter crash off the coast of San Diego was not pilot error but caused by the mechanical failure of a hose funneling hydraulic fluid to the helicopter’s rotor.

The 23-page command investigat­ion by the Navy’s 3rd Fleet was released this week and chronicles events that led up to the Aug. 31 crash of the MH-60S Seahawk helicopter as it landed on the USS Abraham Lincoln during the third of four planned training exercises.

The aircraft fell into the ocean shortly after landing on the ship’s deck; five sailors died. One crew member was later rescued from the ocean.

All aboard the aircraft belonged to the Helicopter Sea Combat Squadron 8 based at North Island, San Diego.

Two of those who died were from Virginia: Lt. Paul R. Fridley, 28, a pilot from Annandale; and Naval Air Crewman (Helicopter) 2nd Class James P. Buriak, 31, from Salem

“The investigat­ion found that there is no evidence that pilot or aircrew error was a causal factor in the crash,” Cmdr. Zach Harrell, a spokespers­on for Naval Air Forces, said.

Investigat­ors said in the report “the crash was caused by an in-flight failure of a damper hose, resulting in total loss of the main rotor damping, which led to severe vibrations upon touchdown.”

The hose feeds hydraulic fluid to the rotary assembly. If the hydraulic fluid is interrupte­d, it can cause instabilit­y in the rotor.

As the helicopter tried to land on the flight deck, it “experience­d lateral and vertical vibrations,” investigat­ors said. As vibrations intensifie­d the helicopter “rotated 50 degrees vertically left and then 200 degrees to the right.”

Then the helicopter’s blade hit the flight deck and it fell into the ocean on the starboard side, sliding tail first.

Witnesses told investigat­ors the helicopter’s approach to land appeared normal and that it hovered 10 feet over the ship before landing. As it touched down, vibrations inside “became violent and the noise level significan­tly increased during touchdown,” the report said.

As the helicopter went overboard, video from the flight deck showed the pilots’ doors were closed, cabin doors were closed and all aircrew members were restrained. A door near the gunner was open, which allowed one crewman to escape, Harrell said.

“The damper hose failed in-flight due to flattening of steel braid strands,” the investigat­ors said in their report. “Bending the hose crushed wire braids into each other, causing flattening and nicking that resulted in fatigue failure of the steel braid strands.”

Investigat­ors said the hose likely failed over time as the helicopter logged more flight hours.

“Records dating back to 2011 do not document a yellow damper hose replacemen­t and the flattening likely happened due to a one-time event at some point,” investigat­ors concluded.

The report says the Navy has taken steps to prevent hose damage due to kinking from occurring in the future.

The helicopter and its crew were found 5,000 feet below the ocean’s surface on Oct. 8 by a Navy salvage and diving team.

 ?? IAN KINKEAD/US NAVY VIA AP ?? An MH-60S helicopter, similar to the one pictured, its two pilots and three other sailors were lost in an Aug. 31 accident about 69 miles off the San Diego coast.
IAN KINKEAD/US NAVY VIA AP An MH-60S helicopter, similar to the one pictured, its two pilots and three other sailors were lost in an Aug. 31 accident about 69 miles off the San Diego coast.

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