Los Angeles Times

United finds loose bolts on planes

Boeing Max 9 jets are grounded as inspectors examine door plugs. Flight ‘black box’ erased.

- By Matt Hamilton and Jeremy Childs

United Airlines investigat­ors found loose bolts and other door plug installati­on issues when investigat­ing their fleet of Boeing 737 Max 9s — potential clues to indicate how the same piece of fuselage blew out on a recent Alaska Airlines flight.

Both United and Alaska have grounded their fleets of the commercial airplanes and canceled hundreds of flights in the aftermath of the incident, which occurred on Alaska Airlines Flight 1282 from Portland Internatio­nal Airport to Ontario on Friday night.

The aircraft had reached about 16,000 feet elevation when the cabin underwent “explosive decompress­ion,” according to Jennifer Homendy, chair of the National Transporta­tion Safety Board, and the door plug burst off the side of the plane.

Among revelation­s at a Sunday night news conference, the NTSB chief said the door plug the agency had been searching for had been found by a Portland, Ore., teacher in his backyard.

“Thank you, Bob,” Homendy said.

The teacher, referred to only by his first name, contacted the NTSB via email and sent two photos of the piece of fuselage, which was described as a 63-pound piece of the plane that is yellow-green in color on one side and white on the other. Two cellphones that plummeted from the aircraft also were found in the vicinity.

In addition, Homendy said that before Friday’s midair incident, the plane had been restricted from long flights over water because of a warning light that had gone off at least three times in the last month, possibly indicating a pressuriza­tion problem on the aircraft.

“We don’t know that there was any correlatio­n” between the warning lights and what happened during Friday night’s flight, Ho

mendy said. But Alaska Airlines had restricted that jet from transconti­nental routes so that the plane could return to an airport during an emergency, she said.

Because the pressuriza­tion light had gone off several times, additional maintenanc­e was ordered on the plane, but it had not been performed before Friday’s flight.

United’s investigat­ion is not the first time loose bolts have been discovered on Boeing 737 Max 9 jets; in late December, Boeing issued a warning to all airlines with 737 Max planes to inspect the aircraft for possible loose bolts in the rudder-control system after an airline reported a missing nut while conducting routine maintenanc­e.

Boeing President and Chief Executive David Calhoun sent a companywid­e email Sunday canceling the organizati­on’s annual leadership retreat to instead host a “safety webcast” with members of the executive leadership team.

“While we’ve made progress in strengthen­ing our safety management and quality control systems and processes in the last few years, situations like this are a reminder that we must remain focused on continuing to improve every day,” the email read.

Federal officials also pointed out a major obstacle to the Alaska Airlines investigat­ion Sunday night: The cockpit voice recorder, or black box, from the Friday night flight was erased.

Homendy said that after the aircraft returned to Portland Internatio­nal Airport, no one pulled the circuit breaker on the cockpit voice recorder or otherwise preserved the audio, which holds only its most recent two hours.

“The cockpit voice recorder was completely overwritte­n. There was nothing on the cockpit voice recorder,” Homendy said.

Homendy was visibly exasperate­d by the loss of the black box recording. She noted that it was a “very chaotic event” when the plane landed and officials set up an emergency operations center.

“The maintenanc­e team went out to get [the cockpit voice recorder], but it was right at about the two-hour mark,” she said, later adding: “We have nothing.”

She pointed to about 10 other recent incidents when voice recorders were overwritte­n, including a 2017 near-catastroph­e at San Francisco’s airport when an Air Canada plane almost landed on a taxiway and would have collided with other jets carrying about 1,000 passengers. She called on the Federal Aviation Administra­tion and Congress to implement a rule that would require planes to store audio for 25 hours, which aligns with European audio-retention practices.

“If that communicat­ion is not recorded, that is unfortunat­ely a loss for us and a loss for FAA and a loss for safety,” she said, “because that informatio­n is key.”

Alaska Airlines did not respond to questions about the cockpit voice recorder or whether the airline would voluntaril­y install recorders that store audio for 25 hours.

Asked to offer any theories about what caused the plane’s door plug to blow off, Homendy demurred.

“Right now we are in a fact-finding phase of the investigat­ion,” the NTSB chief said, adding that staff were poring over the Boeing 737 Max 9 aircraft for clues and planned to send key components to a lab to analyze any fractures, paint marks and shearing that could help explain what happened.

Surveying the aircraft, officials found damage in more than a dozen rows inside but had not identified any structural damage to the aircraft. The plug that blew off the plane was covering an unused emergency exit opening near Rows 25 and 26, and was essentiall­y bolted to the aircraft structure. The plug was covered in paneling and included a window so that, from inside the cabin, it would appear indistingu­ishable from other rows.

On Monday, investigat­ors had planned to examine the door plug on the other side of Rows 25 and 26 to try to determine what caused the other plug to blow off.

Homendy on Sunday praised the flight attendants and pilots for a quick response in an environmen­t that was terrifying and marred by communicat­ion problems.

Passengers and crew reported hearing “a bang,” she said, when the “explosive decompress­ion” occurred after the plug was expelled from the fuselage.

“It was described as chaos, very loud,” she said. The cockpit door flew open, and the captain partly lost and first officer completely lost their respective headsets.

“Flight attendants reported that it was difficult to get informatio­n from the flight deck, and the flight deck was also having difficulty communicat­ing,” Homendy said.

The plane had six crew members and 171 passengers, including three babies and four unaccompan­ied minors.

“The flight attendants were very focused on what was going on with those children. Were they safe? Were they secure?”

In a stroke of luck, two seats were empty directly next to the spot where the hole opened in the plane.

Seats in that area showed signs of damage, including sheared oxygen masks, lost headrests and torquing.

“There was a lot of damage to the interior paneling and trim,” she said. “It must have been a terrifying event to experience.”

 ?? David J. Phillip Associated Press ?? DAYS AFTER a midair incident involving an Alaska Airlines Boeing 737 Max 9 jet, United Airlines found loose bolts and other door plug issues when examining its own f leet of the planes, which are now grounded.
David J. Phillip Associated Press DAYS AFTER a midair incident involving an Alaska Airlines Boeing 737 Max 9 jet, United Airlines found loose bolts and other door plug issues when examining its own f leet of the planes, which are now grounded.

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