SAIL

RUDDER REBUILD

A hard grounding leads to a summer of discontent for Nigel Calder

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Nigel Calder reports on the complexiti­es of a major repair following a hard grounding

While cruising the coast of Portugal last summer, I drove Nada, our Malo 46 sailboat, hard onto a sandspit in 3ft breaking seas. All Malos are exceptiona­lly strongly built, so I was not immediatel­y concerned about the hull. The rudder, however, was taking a beating as it hit the bottom in every wave trough. Nonetheles­s, we made it into deeper water with the rudder still working.

From there we had an easy three-hour motorsail to Baiona, Spain, which had the nearest boatyard with a Travelhois­t. We then arranged a haulout to check for damage, which proved to be much worse than we expected.

The first task was to find someone to repair the boat. This was theoretica­lly easy in as much as a service and repair company, RoNautica, also operated in the boatyard, and it was not safe to move Nada. However, almost nobody spoke English, and the outfit looked pretty rinky-dink, with no proper workshop on site and what appeared to be poor shop practices. Although I was assured that the fiberglass technician, Rubio, was highly experience­d, I could not tell whether he or anyone else was familiar with our type of rudder.

The Spanish surveyor hired by Pantaenius, our insurance company, also spoke very little English. Nonetheles­s, he made a perfunctor­y visual inspection of the damage, after which he and RoNautica discussed the repair and came up with a plan of action. We were promised the repair could be completed in two to three weeks and would be stronger than the original constructi­on. In the meantime, my wife, Terrie, and I would not be allowed to camp out on Nada, so we found the first of several Airbnb’s and moved ashore.

In 35 years of cruising, we have never made an insurance claim. I was under the impression the surveyor hired by the insurance company would act as a project manager. However, I was politely informed that it was my responsibi­lity to hire the workers, get an estimate for the repairs and then sign off on them when they were done. It was also my job to act as project manager. If I wanted someone else to do this (such as the surveyor) I was informed I would have to contract for this and pay for it separately. Apparently, the surveyor’s only job was to make sure the estimate was acceptable.

WORK BEGINS

The rudder was removed the day after the surveyor came. As a result of the grounding, it was now partially curved along its length and split apart on the top and forward seams, which meant the two halves needed to be pried apart to effect a repair. At this time our primary mediator with RoNautica, Alex, took off for a week’s holiday. It was then several days before we could persuade anyone to attempt to split the rudder, during which time nothing was done. Terrie and I were quickly getting frustrated.

Finally, a delightful­ly cheerful fellow, Jose, attacked the seam with a cold chisel and hammer: so vigorously, in fact, that I worried he might do permanent damage to the surroundin­g laminate. I supplied an angle grinder from among our onboard tools; he supplied a considerab­le number of wooden wedges; and the job was done in a couple of hours—Jose grinding away in a cloud of fiberglass dust without protective clothing, periodical­ly driving in wedges with gusto.

After that the two shells needed to be thoroughly cleaned. Again, RoNautica had no shop on-site, so the work was done outside under a portable awning. At this point, Rubio took over from Jose. Unfortunat­ely, we discovered that Rubio, though meticulous, was frequently distracted, and it was a good day if he got in four hours of work. In the end the job took a week. Terrie and I would happily have done the work in a day, but couldn’t see a way to insert ourselves into the process without causing offense.

PARTS AND PIECES

In addition to repairing the rudder itself, we also needed new seals and a bearing for the rudder tube. The original assembly had been built by the Danish company Jefa, so I contacted them and discovered that although Malo has effectivel­y been out of business for a decade, Jefa still had all the parts. I was warned, though, that Jefa was shortly to go on its annual vacation, which in Europe is typically a month. Jefa also wanted payment before sending anything, which I could see taking several days and running us into the vacation period, at which point we would be well and truly stuck. The bills from staying ashore were also now piling up, and friends were due to fly in and join us in a couple of weeks. I therefore told Jefa I would pay for the parts and sort it out later with the insurers.

Alex returned that Monday, and we had a bit of

a meltdown over the fact the promised work had not yet begun on the hull repairs. Perhaps because of the resulting argument (or perhaps it was all part of the plan and simply a matter of language difficulti­es) the next morning, 10 days after the rudder had been removed and work had technicall­y commenced, we finally got on a roll. Two weeks later we thought we were done.

In one sense we had been lucky. In spite of the primitive working conditions, it became clear that Rubio was not only experience­d with fiberglass but extremely conscienti­ous. The repair of both the rudder and hull was done with considerab­le skill. Considerin­g we’d had the accident immediatel­y before the start of the summer vacation season in Europe, we’d also been remarkably lucky to have found the labor and repair parts we needed, not to mention get the job done, in just over three weeks. We parted with RoNautica on good terms.

NOT SO FAST...

From there it was across the somewhat notorious Bay of Biscay to northern France. The trip began as a quiet motorsail in light winds and calm seas, but ended with 30-knot winds gusting to 40, and rough seas and considerab­le rudder loads. As this was happening Nada began taking on water, bubbling up through the base of a limber hole close to the rudder-repair area. I had a theory on how the water was getting in that, if correct, meant we had no serious structural problems. However, I was not about to attempt any further repairs in a country where we could not speak the language.

After holing up in a marina in France to wait until the gale blew itself out, we motorsaile­d to Falmouth, England, at the same time letting Pantaenius know we had a leak. Pantaenius then contacted a local surveyor, David Cox, who showed up as soon as we arrived in Falmouth and immediatel­y had us hauled by the Falmouth Boat Company (FBC).

Unfortunat­ely, the minute the hull emerged from the water, we could see we had a serious problem: the antifoulin­g paint, which had only been put on a couple of weeks earlier, was now missing at the junction between the skeg with the hull. We also found we could now flex the skeg and rudder from side to side by hand, with water dribbling out of the cracks that had now opened up around them. My theories as to the source the leak were completely wrong. The Spanish repair job had failed, but what exactly had happened?

David suspected delaminati­on deep within the hull layup. He also speculated that the RoNautica repair had not cut back into the hull deep

enough, either internally or externally, to reveal this delaminati­on and as such had failed to re-establish a bond between the hull skin (of which the skeg and lower rudder bearing are a part) and the skin inboard of the skeg to which the rudder tube and support structure are attached. In short, under load the skeg had flexed independen­tly of the rudder tube structure, ultimately cracking RoNautica’s new hull laminate.

Core samples were cut at four different points around the skeg, and even though Nada had been out of the water for several days, water still dribbled out from the holes that were made. All four core samples also exhibited substantia­l delaminati­on within and between the hull and inner skins, so much so it was decided it was not repairable—the skeg and the hull area around it would both have to be cut out and rebuilt from scratch.

WORSE YET

As a first step, I obtained the specificat­ions for the original hull laminate to ensure the new structure would make a good match. FBC then lined the exterior of the hull and existing skeg with a mold release agent and laminated a mold up against the hull and skeg complete with locating lugs. That done, the mold was popped off the hull and a new skeg vacuum-bagged inside it using Malo’s original laminate schedule and epoxy resin.

Meanwhile, at the same time all this was going on, the interior of the boat around the rudder tube and skeg area was also disassembl­ed. This involved removing various hoses, the steering system, the hot water tank, the central heating system (this is a Swedish boat!) and numerous cables and other fittings. The bonded-in cockpit drains were also cut out along with a couple of major bulkheads and some interior structures cut back.

After that, the skeg and surroundin­g hull area were cut out of the boat, in the process revealing yet more internal damage: damage so bad an 8in plastic cable tie could be fully inserted between the layers of hull laminate. A bigger hole therefore needed to be cut in the hull and the aft starboard cabin disassembl­ed to remove Nada’s fuel tank to provide access to the work area—this despite the fact the repair job was already way over budget.

Meanwhile, as the bad news regarding the hull continued to pile up, FBC turned its attention to the rudder, which had been extensivel­y rebuilt during the Spanish repair but without correcting a significan­t bend that now caused substantia­l steering loads when under power. Upon inspection, it was decided the rudder could be partially cut back and faired to restore the correct profile. However, accurate measuremen­ts were first needed. Soon afterward I received another e-mail from Jonathan Fielding, the head of FBC: “Having now been able to fully assess and measure the rudder, it is in an awful state regarding the profile … Can we discuss this when you have a moment to call as I am thinking we ought to simply make another blade and solve the problem once and for all.” In the end, the rudder had to be completely rebuilt.

TURNING THE CORNER

Back aboard the boat itself, the hull having now been cut and feathered back to the limit of the delaminati­on, the new skeg, still inside its mold, was lifted up into place, using the locating lugs left on the undamaged hull to ensure it was correctly located. The skeg was then vacuumbagg­ed in place with multiple layers of laminate based on Malo’s original hull specificat­ions, with some additional carbon fiber reinforcem­ent added for good measure. After that it was filled and laminated over. Areas of core that had been cut away were restored and the inner skin vacuum-bagged into place.

After that the now completely rebuilt rudder was lifted up and positioned on the bearing at the lower end of the new skeg. The rudder tube and upper bearing were then slid onto the shaft from above and bonded into place with substantia­l rudder tube reinforcem­ent. When the job was complete, the rudder could be turned with the tip of a finger.

Finally, it was time to begin reassembli­ng Nada’s interior, after which the job was complete—five months after we had been hauled out, and

100 percent over budget because of the considerab­ly greater area of delaminate­d hull that had been detected. Soon afterward, Terrie and I flew back to the UK to inspect the work and to do sea trials, which went perfectly. We had our Nada back.

It had been a long haul, but in retrospect I realized we had been extremely lucky. Sooner or later the first repair job would have failed. And had the near gale in the Bay of Biscay not cracked the hull-to-skeg joint when it did, the failure might have occurred in worse conditions further offshore, resulting in the loss of Nada and even loss of life.

Nada is once again good to go. What is not so easily repaired is Terrie’s confidence in my navigation­al abilities!

 ??  ?? After running hard aground the Malo 46 Nada required extensive repairs
After running hard aground the Malo 46 Nada required extensive repairs
 ??  ?? Glassing the damaged skeg in Spain: it wouldn’t be enough
Glassing the damaged skeg in Spain: it wouldn’t be enough
 ??  ?? Splitting the damaged rudder early on during repairs in Spain
Splitting the damaged rudder early on during repairs in Spain
 ??  ??
 ??  ?? Cutting core samples (left) and the seepage the resulted
afterward (below)
Cutting core samples (left) and the seepage the resulted afterward (below)
 ??  ?? Cleaning out the rudder structure
prior to rebuilding
in Spain
Cleaning out the rudder structure prior to rebuilding in Spain
 ??  ?? The state of the
rudder tube immediatel­y after
the grounding
The state of the rudder tube immediatel­y after the grounding
 ??  ?? Installing the repaired rudder
back in Spain
Installing the repaired rudder back in Spain
 ??  ?? Half the rudder,
now ready for rebuilding
Half the rudder, now ready for rebuilding
 ??  ?? Pouring new foam into the interior of the rebuilt
rudder
Pouring new foam into the interior of the rebuilt rudder
 ??  ?? In the UK, workers created a robust
shelter around the damaged area
In the UK, workers created a robust shelter around the damaged area
 ??  ?? The mold for the new skeg after being popped off the hull
The mold for the new skeg after being popped off the hull
 ??  ?? A view of the the top of the damaged rudder on
the hard in Spain
A view of the the top of the damaged rudder on the hard in Spain
 ??  ?? The original skeg, which ended up having to be
replaced
The original skeg, which ended up having to be replaced
 ??  ?? A closeup of a damaged core sample: not good!
A closeup of a damaged core sample: not good!
 ??  ?? The new skeg mold after being
removed from the hull; vacuumbagg­ing the new
skeg (inset)
The new skeg mold after being removed from the hull; vacuumbagg­ing the new skeg (inset)
 ??  ?? Preparing the hull and skeg as a first step to creating the new mold
Preparing the hull and skeg as a first step to creating the new mold
 ??  ?? Adding a carbon layer in the area of the skeg attachment
Adding a carbon layer in the area of the skeg attachment
 ??  ?? The new skeg in place, ready for priming and painting
The new skeg in place, ready for priming and painting

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