The Day

Jetliner that lost door part was being monitored

Alaska Airlines knew pressuriza­tion warning light had gone on 3 times before near-tragic flight

- By CLAIRE RUSH and DAVID KOENIG

Portland, Ore. — The Boeing jetliner that suffered an inflight blowout over Oregon was not being used for flights to Hawaii after a warning light that could have indicated a pressuriza­tion problem lit up on three different flights.

Alaska Airlines decided to restrict the aircraft from long flights over water so the plane “could return very quickly to an airport” if the warning light reappeared, Jennifer Homendy, chairwoman of the National Transporta­tion Safety Board, said Sunday.

Homendy cautioned that the pressuriza­tion light might be unrelated to Friday’s incident in which a plug covering an unused exit door blew off the Boeing 737 Max 9 as it cruised about three miles over Oregon.

On Monday, the Federal Aviation Administra­tion approved guidelines for inspecting the door plugs on other Max 9 jets and repairing them, if necessary. That move should speed the return to service of 171 planes that the FAA grounded under an emergency order Saturday.

Alaska has 64 other Max 9s, and United Airlines owns 79 of them. No other U.S. airlines operate that model of the Boeing 737.

The auto-pressuriza­tion system warning on the ill-fated Alaska Airlines jet lit up during three previous flights. Homendy said she didn’t have details about a Dec. 7 incident, but that it came on again during a flight on Jan. 3 and after the plane landed on Jan. 4 — the day before the blowout.

“We plan to look at that more, and we’ve requested documentat­ion on all defects since delivery of the aircraft on Oct. 31,” she said.

The NTSB said the lost door plug was found Sunday near Portland, Ore., in a the backyard of a home. Investigat­ors will examine the plug, which is 26 by 48 inches and weighs 63 pounds, for signs of how it broke free.

Investigat­ors will not have the benefit of hearing what was going on in the cockpit during the flight. The cockpit voice recorder — one of two so-called black boxes — recorded over the flight’s sounds after two hours, Homendy said.

At a news conference Sunday, Homendy provided new details about the chaotic scene that unfolded on the plane. The explosive rush of air damaged several rows of seats and pulled insulation from the walls. The cockpit door flew open.

The force ripped the headset off the co-pilot and the captain lost part of her headset. A quick reference checklist kept within easy reach of the pilots flew out of the open cockpit, Homendy said.

 ?? NATIONAL TRANSPORTA­TION SAFETY BOARD VIA AP ?? National Transporta­tion Safety Board Investigat­orin-Charge John Lovell examines the fuselage plug area of Alaska Airlines Flight 1282 Sunday in Portland, Ore. A panel used to plug an area reserved for an exit door on the Boeing 737 Max 9 jetliner blew out Friday night shortly after the flight took off from Portland, forcing the plane to return to Portland Internatio­nal Airport.
NATIONAL TRANSPORTA­TION SAFETY BOARD VIA AP National Transporta­tion Safety Board Investigat­orin-Charge John Lovell examines the fuselage plug area of Alaska Airlines Flight 1282 Sunday in Portland, Ore. A panel used to plug an area reserved for an exit door on the Boeing 737 Max 9 jetliner blew out Friday night shortly after the flight took off from Portland, forcing the plane to return to Portland Internatio­nal Airport.

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