Project MG Midget
This issue, the front suspension, steering and brakes of our Mk3 project Midget are stripped, assessed and then built back up.
As we explained last issue, after the extensive bodywork repairs to date, we need to pick up the pace on this Midget project if we are to bring it to a conclusion in the planned 12 chapters. That means skipping ahead on some of the mechanical aspects, but that is no big deal because these are adequately covered in the workshop manual. So instead of attempting to recreate the whole stepby-step sequence of each job, we will aim instead to give a flavour of the work, and to highlight any issues we found or any little tips that might help you.
This time around we are looking at the front brakes and suspension. Overall, the mechanical condition of the Midget was pretty good, and a credit to the previous long-term owner. We did find one or two aspects that could be improved, and we also replaced a few items with new that could reasonably have been salvaged – sometimes you do have to calculate the work involved in reclamation compared to replacement, and often the conclusion you reach will depend on your mood at the time, or how many big bills you have just paid out! There is also the danger of mission creep that we have mentioned previously, with standards rising and some
items being discarded because new parts will look better rather than because the old ones positively need to be replaced.
It was back in the March issue that we decided the front suspension and steering had to come off the car so that the entire engine bay could be grit blasted back to bare metal. Each side came off as a complete unit of wishbone, stub axle, brake caliper and disc, kingpin and trunnion link. I separated the lever arm dampers which formed the top links and removed the springs – these were inspected, but found to be fine and so just cleaned up and painted. The rest of the assemblies were taken to the work bench for further dismantling.
One general tip when working on items like this that have not been disturbed for many years and lived in a particularly harsh environment is to use a six-point socket rather than a 12-point one whenever you can to reduce the chances of it slipping and rounding off a rusty fixing. Before even attempting to undo anything stubborn though, clean off any exposed threads with a wire brush in a drill, and spray on plenty of penetrating fluid. Then, after this has had time to soak in, use a breaker bar or long ratchet and see if it will turn – heat and/or shock tactics might be needed, but a long bar will often do the trick, allowing you to apply firm and sustained pressure to loosen things off without needing to resort to anything more potentially destructive. However, if that doesn’t work and you don’t have a gas torch to apply high and concentrated heat, try shocking it free with an impact screwdriver, then undo the fixing a couple of flats, wind it back on, spray on more fluid, then undo it a couple more turns. It is a slow and laborious process, but generally much quicker than having to drill out a fixing that has sheared.
Another tip is never to throw anything out until the entire job is done, even if something is certain to be replaced. That’s because it could be useful to refer back to the old part and ensure the new one
is correct, or to spot any differences if something is reluctant to go back as it should. The old bits will also have various wear and grime marks that can aid with the correct orientation of parts and reminding you how they fit together.
With everything cleaned on our suspension, the parts could be checked and either replaced or prepped and painted as necessary. The king pins and bushes were a nice snug fit together, so they could go back in. The dampers were in good shape too, with plenty of smooth resistance when the arms were moved by hand. The springs and seats were also good to go, although – as detailed in the pictures – new wishbones were fitted.
I also intended to fit new wishbone bushes, but the ones I’d bought did not fit between the mounting flanges on the body. I tried adding red grease to the faces of the bushes to help them slide in, really squeezing the bushes hard and levering the mounting brackets slightly further apart, but all this did was damage the paint. After half an hour of fruitless toil, I took the wishbone back to the bench and compared the new bushes with the old ones. It turns out that the lip of the new bushes was at least twice as thick as the old ones had been. Since the old bushes were actually in good shape and I only replaced them for the sake of completeness, I swapped them back over and the wishbone slipped into the mounting lugs with just enough pressure to create a nice, snug fit.
With the wishbone finally fitted, I took the upright that I had previously built up and attached that to the outer end of the wishbone at the bottom and to the damper arm at the top. There is a pinch bolt that goes through the end of the damper arm, and a corresponding groove in the trunnion pin. As this can be hard to
see through the hole with all the grease in there, I marked the pin head with a dot of Tippex so that I knew when the groove was facing in the right direction.
I now wanted to fit the spring, and realised I had to take the lower spring seat back off the wishbone. That’s because there is an ingenious way of fitting the front spring on a Midget that doesn’t require the use of spring compressors.
I had already bought some high tensile bolts the same diameter as the spring seat bolts, but much longer at 4½in. The trick then is to insert the spring up through the hole in the wishbone and into its seat around the bumpstop at the top. The lower seat is then attached underneath the wishbone with the two long bolts in diagonally opposite securing holes, and tightening these up evenly pulls the seat up against the wishbone, compressing the spring in the process. Once metal was against metal, I could fit two of the regular bolts in the remaining two holes, before removing the long bolts and replacing them with two more regular ones.
Next up, the hub and disc brake went back on, followed by the brake caliper. I had new calipers and dust shields, and could not get the two mounting bolts to engage in the corresponding threaded holes in the stub axle. It was a little tricky anyway because the bolt goes through a tab washer, brake hose lock plate, dust shield tab and the caliper itself before reaching the hub, and you have little hope of being able to see where the threaded hole is through all these. The picture sequence shows where my problems lay.
After finding and fixing this problem, everything went back on fine and I was on the home straight, but not quite finished yet. The next problem was of my own making, because I had already assembled the steering rack and fitted that, but now the track rods would not drop down far enough for me to insert the track rod end up and into the steering arm. Naturally enough I was not keen on dismantling anything again, so I hit on the easiest solution: I removed the TRE, fitted this to the steering arm and then wound the track rod itself into the TRE.