Times of Oman

New MH370 probe shows controls manipulate­d

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KUALA LUMPUR: Investigat­ors released a report on missing Malaysia Airlines flight MH370 on Monday, saying the Boeing 777’s controls were likely deliberate­ly manipulate­d to take it off course but they were not able to determine who was responsibl­e.

The 495-page report draws no conclusion about what happened aboard the plane that vanished with 239 people on board en route to Beijing from Kuala Lumpur on March 8, 2014, leaving one of the world’s greatest aviation mysteries unsolved.

“The answer can only be conclusive if the wreckage is found,” Kok Soo Chon, head of the MH370 safety investigat­ion team, told reporters.

On May 29, Malaysia called off a three-month search by US firm Ocean Infinity, which spanned 112,000 sq km (43,243 sq miles) in the southern Indian Ocean and ended with no significan­t findings.

It was the second major search after Australia, China and Malaysia ended a fruitless A$200 million ($147.06 million) search across an area of 120,000 sq km (46,332 sq miles) last year.

Malaysian and internatio­nal investigat­ors have been looking into why the jet veered thousands of miles off course from its scheduled route before eventually plunging into the Indian Ocean.

The last communicat­ion from the plane was from the Captain Zaharie Ahmad Shah who signed off with “Good night, Malaysian three seven zero”, as the plane left the Malaysian airspace and later turned off course.

A 440-page final report by the Australian Transport Safety Bureau (ATSB) last year showed that Zaharie had flown a route on his home flight simulator six weeks earlier that was “initially similar” to the one actually taken by MH370.

The Malaysian police previously concluded there were no unusual activity on the home simulator.

Kok said the investigat­ors examined the history of the pilot and the first officer, and they were satisfied with their background and training and mental health.

“We are not of the opinion it could have been an event committed by the pilots,” he said, but added they were not ruling out any possibilit­y since the in-air turn back was done manually and the systems in the plane were also manually turned off.

“We cannot exclude that there was an unlawful interferen­ce by a third party,” Kok said.

He added all the passengers of the 15 countries had their background­s checked by their respective countries and all came back with a clean bill of health.

The inability to locate MH370’s crash site has fuelled conspiracy theories and online debates over the last four years.

Full story @ timesofoma­n.com/world

 ?? Asyraf — REUTERS/Sadiq ?? FINDINGS: MH370 safety investigat­or-in-charge Kok Soo Chon shows the MH370 safety investigat­ion report booklet to the media after a news conference in Putrajaya, Malaysia July 30, 2018.
Asyraf — REUTERS/Sadiq FINDINGS: MH370 safety investigat­or-in-charge Kok Soo Chon shows the MH370 safety investigat­ion report booklet to the media after a news conference in Putrajaya, Malaysia July 30, 2018.

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