Popular Mechanics (South Africa)

WIND, SUN AND DEEP CYCLE

No experience fixing up a sailboat? No problem

- BY IAN MCNANIE PHOTOGRAPH­S BY JUSTIN KAN EPS

I’D NEVER SAILED BEFORE. This wasn’t a problem, however, because we were not sailing. We were hobbling. My new boat, bought for R58 000 from a man who told us only after we’d paid that we had two days to move the boat before he was kicked out of his slip, puttered out of the Alameda Channel and into San Francisco Bay. A 1974 Tartan 34C, No Bubbles fulfilled the promise of its name. At full throttle, the 10,4 kw outboard motor I’d lashed to the transom moved us wakelessly toward the Oyster Point Marina, 16 km across the bay. It would take six hours to get there.

When I bought No Bubbles, I knew it needed work. The previous owner had taken the engine out to do repairs and left it in a dock cart for months, where it rusted into oblivion. And that was a problem I could actually see. But I wasn’t deterred. I work as an intern with former Mythbuster Jamie Hyneman, who offered unlimited tools and advice. His shop has everything you need to build anything, and he spent years sailing a dive boat in the Caribbean. I also work at a robotics company. Between the two, I knew I could handle the project – especially since I’d decided to completely replace the shot motor with an electric one. Here’s how I did it.

Propulsion At my electronic­s job, we

were working with brushless 30 kw, scaled-up permanent magnet drone motors which are much smaller and more powerful than similarly sized induction motors. The motors are designed for DIY projects like airplanes and cars, and after writing custom firmware for one and troublesho­oting the powertrain, I decided to order a 27 kv version for my sailboat. “KV” is a constant that approximat­es the rpm the motor will spin per volt applied to it. If I multiply kv (rpm/ V) by my target voltage (80 V), I can predict that, unloaded, the motor will spin at about 2 160 r/min. Loaded, this puts it in a similar range to the boat’s original Atomic 4 engine. To control it, I added a 500 A electronic speed controller (ESC) from Alien Power System hooked up to an RC transmitte­r.

One benefit presented itself before I even hit the water: The Tartan was designed with the motor right in the middle of the cabin. It takes up a lot of room. To walk through, you have to squeeze around the engine cover. But with the new tiny motor, which is only 15 centimetre­s in diameter and eight centimetre­s thick, I could replace the engine cover with a small step and regain all of that floor space.

Prop Shaft Jamie helped me attach

the motor to the prop shaft. We figured it would probably have enough torque to start moving the prop, so I made it direct drive for now, with no gear reduction. But if the bilge filled up and the bilge pump failed, that would leave the motor submerged The salt water would destroy the bearings instantly To avoid that, I built a small plexiglass box around the motor to keep the water out.

Power The motor runs on six

12 V 66 Ah deep-cycle batteries in series. On a calm day, it draws about 30 A at about three knots. To make the boat go faster, I’ll eventually need to change the prop, up the voltage, and get a new ESC that can handle it.

I also found eighteen solar panels on Craigslist for only R2 per watt. Jamie and I welded an aluminium frame in an arch above the companionw­ay, where we mounted five of the panels – power supply and an awesome rain shield. During peak sun, the panels can provide 375 watts. That’s fine for charging my house pack, which runs the basic electrical components of the boat, but the motor batteries still need to connect to shore power. Eventually I’ll cover the boat in the remaining panels and add a 3 500 W Harbor Freight inverter generator. That should provide enough power to run the boat most of the time.

Chainplate Knees Chainplate­s are metal

supports that poke through the deck for the rigging wires to clip to. They’re bolted to pieces of wood attached to the hull. The compartmen­t surroundin­g the starboard knee was completely filled with water. Once I cut out the fiberglass around it, the plywood was so rotted I could scoop it out with my hands. I cut a new piece of wood, and Jamie gave me some fiberglass, epoxy, and filler to seal it back in. My biggest mistake was forgetting gloves. Getting the bits of epoxy out of my arm hair afterward might have been the hardest part of getting No Bubbles back on the water.

 ??  ??
 ??  ??
 ??  ?? A metal terminal block connects the electronic speed controller to the motor phases.
A metal terminal block connects the electronic speed controller to the motor phases.

Newspapers in English

Newspapers from South Africa