Arkansas Democrat-Gazette

Agency details I-40 bridge fallout

Employees retired, not fired, out of compassion, it says

- STEPHEN SIMPSON

Officials with the Arkansas Department of Transporta­tion told legislator­s Wednesday the decision to allow two veteran employees to retire instead of being outright terminated for their role in the months-long closing of the Interstate 40 bridge at Memphis was an act of compassion instead of an attempt to mislead the public.

Lorie Tudor, transporta­tion director, presented to the Highway Commission Review and Advisory Subcommitt­ee the results of the department’s investigat­ion into how the structural fracture at one of the state’s major bridges was overlooked.

The results of the agency’s investigat­ion, a Federal Highway Administra­tion review and a forensic analysis of the fracture all led department leaders to conclude that among the “changes/ enhancemen­ts to strengthen and improve” the bridge inspection program was placing the heavy-bridge maintenanc­e section “under new management,” according to an After Action Report that the department prepared.

Rep. David Ray, R-Maumelle, asked Tudor if the retirement of Steven Hill, the heavy-bridge engineer and a 26-year agency veteran, as well as his assistant, Stewart Linz, a 36-year veteran, were connected to this report that concluded a failure in management when it came to bridge inspection.

Their section was responsibl­e for inspecting and maintainin­g 60 of the largest and most unusual bridges in Arkansas, including the I-40 bridge connecting West Memphis and Memphis.

Tudor confirmed both were given the option to retire after they were found to

be responsibl­e for the failure to catch the fracture earlier.

“We felt they didn’t manage the program the way it should have been and that is the reason why we felt new management was needed to move forward,” she told the legislativ­e body.

Rep. Frances Cavenaugh, R-Walnut Ridge, questioned Tudor on the reason the two engineers were even given the option to retire.

“Why didn’t we terminate somebody for a job that could have cost millions of dollars and human lives?” she asked.

Tudor said they felt it was the decent thing to do.

“They were good engineers and it wasn’t done intentiona­lly,” she said.

The two retirement­s came after the dismissal in May of Monty Frazier, the bridge inspector who missed the crack during inspection­s in 2016, 2017, 2019 and 2020.

The 2018 inspection was performed by an inspector who had never examined the affected part of the bridge. He since has been counseled and will receive more training.

The review found that the culture fostered by heavybridg­e maintenanc­e program management allowed shortcomin­gs and shortcuts to be overlooked and suggested Frazier’s deficienci­es were common knowledge within the program.

“Management’s failure to adequately act on reports by employees concerned with the terminated inspector’s job performanc­e perpetuate­d a culture where team members did not feel they had the authority or support to question a lead inspector’s procedures or thoroughne­ss,” according to the report.

The program also failed to enforce documented procedures for rotating inspection teams.

“The assigned ‘lead’ inspector was rotated and recorded in the system, but the same inspector was allowed to inspect the same arch spans each time in 2016, 2017, 2019, and 2020,” the report found.

Ray said the statement on the two engineers retiring that was released to the press seemed too vague in his opinion since it didn’t go into detail about their responsibi­lity when it came to the bridge closure.

“Shouldn’t you guys have proactivel­y said something about this when it came to their retirement,” he said. “Because if we didn’t ask the questions, this wouldn’t have been made public.”

Tudor said as department officials navigated through this entire process, they wanted to be as transparen­t as possible, but when it came to personnel action, they wanted to take the high road.

“We didn’t want to slam somebody in the press,” she said “We tried to say it in a way that they can retain some dignity. We could have made it a lot different.”

The partial fracture in the I-40 bridge was discovered by chance by an engineer with Michael Baker Internatio­nal under contract to inspect another portion of the bridge.

The engineer who discovered the crack immediatel­y moved to have the 48-yearold bridge closed to traffic. The bridge, also called the Hernando DeSoto Bridge, is part of a major freight corridor that carries 40,000 vehicles daily, 30% of them big trucks. It took weeks to unsnarl the delays caused by the bridge closing and cost the trucking industry millions of dollars in delays and additional fuel use.

Mississipp­i River barge traffic also was briefly halted to allow time for crews to inspect the bridge and stabilize it.

In all, $10 million was spent to repair and inspect the bridge, according to the department’s after-action report.

After being asked by Rep. Jimmy Gazaway, R-Paragould, Rex Vines, deputy director and chief engineer, told the committee he couldn’t put an exact number on how close the bridge was to “catastroph­ic” failure, but the likelihood was high when the crack was discovered.

“It was very close to system failing,” Vines said.

Robert Moore Jr., chairman of the Arkansas Highway Commission, expressed his confidence in Tudor and the direction of the Department of Transporta­tion to the committee after the investigat­ion was presented.

“We all know we are trying to learn from this situation,” he said. “It has become a catalyst of an in-depth investigat­ion into our bridge program and the director has acted very swiftly. She took ownership for the past and the after-action report summary details the correct actions we need to take and gives us a road map for the future.”

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